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Most viewed - Brian Lantip's Black 1993 Convertible Drivetrain Rehab (COMPLETED) |
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139 views
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139 views
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139 views
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139 viewsready to rock!
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138 viewsStripped balance tube bolt holes retapped
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138 viewsPile Gone!
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138 viewsShiny driveshaft!
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137 views
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135 viewsHolds 4 QTS....that looks to be about 2 that drained out.
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134 views
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134 viewsUpsy daisy!
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133 views
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133 viewsHeatshields removed.
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131 views
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131 viewsclutch fork & ToB reinstalled
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122 viewsUseless water line on a necessary bracket.
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120 views
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118 views
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118 viewsThe remains of a fuel line screw clamp fastening screw, came from inside the #5 runner. That was the fatal screw.
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118 views
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117 viewspurty NEW injectors!
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115 viewsmore useless coolant lines
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112 viewsverified timing.....
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105 views
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105 viewsUseless water line removed from necessary bracket
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104 viewsThe screw pile got bigger. That addition mess is the threaded portion of another screw and what appears to be the torque plate of a fuel line screw clamp. Came out of # 2 runner.
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420 files on 5 page(s) |
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